Pre-rebuild
    At first glance the front to back picture looked like the root tube was bent, but it was just being forced off center by the 2 bent vertical uprights on the left side.
    The main spar on the right wing was bent and would need to be replaced.  Luckily that's all for the wing, and this is one case where it was nice to have Dacron wings verses PolyFiber.  It was very easy to just cut the fabric off the tip, slide the sock off replace the main spar, and slide the sock back on.  Only the end of the wing had to be recovered.
PS: having Jim help made it even easier to fix the wing.
    The entire front wheel assembly needed to be replaced, the fork that was on the plane was steel, wonder what would have happened with a stock aluminum one?
Skinned
    After removing the fabric it was obvious two of the uprights had to be replaced since one was bent to the point of cracking and the other (shown in picture with good tube) was over bent.  It was also interesting that when I cut the fabric off, the two nuts on the cross bolts that hold the front two uprights in place fell to the ground.  Apparently they had never been tightened, and since this Challenger never had the wide body modification, the only thing holding the bolts in was the fabric (elongated hole shown in picture with good tube).  I also had to replace the stringer tube along the bottom on the left side.
    While the plane was skinned, I referred to it as my "terminator plane"
Covering
    Pre-wide body picture shows structure prior to Jim helping add the wide body modification, and the bondo patches on the nose cone to fill low spots from using to strong a stripper to get old paint off.  Learned using wrong stripper on fiberglass is a really bad idea, and set me back a couple weeks patching, and sanding.  The covering pictures are pretty self explanatory, and it was the part that scared me the most, but was the easiest, and quickest part.  "pink plane" is after two coats of PolyBrush to seal and allow paint to stick, "gray plane" is after three coats of Latex primer (thanks to Jims idea of using Latex).

 

Rebuild
    Finally I get to paint it, but wait it's the hottest most humid part of the year, and the paint takes forever to dry "painted blue" is after three coats of blue, and four coats of yellow.  OK now quickly rebuild and I'm done ...NOT.  I noticed the holes in the rudder horns were oversized, ordered two more.  Cut and fitted the wheel struts, and noticed the brackets on the wheel pants were different, so they didn't fit right, also noticed one wheel was very crooked.  Boy I understand why a lot of guys don't put on the wheel struts, they're a pain to work around if you have to take the gear legs on and off.
  I thought the white dash would glare, so I took all the gauges out, and painted it flat black, while the dash is out I'm installing and wiring up a CB that I had in my Rotec Rally.  I'm also wiring up an electric motor to the flaperon tube to make it easier to lower the flaps for short field landings (got info. off internet)
 
PS:  I, lengthened, my runway 100 feet, to 500 feet so I can land the Challenger in my backyard, the Rotec Rally only took about 200 foot of rollout with no brakes, but a stall of about 25mph.  Hopefully with brakes, practice, and electric flaps it will be no problem.
New Dash:
    I removed the old dash and gauges to paint it flat black for glare reduction.  This is the re-installed dash.  Note the CB radio mounted lower left (Marty Spies and I talk on CB while flying).  Below the CB is a yellow toggle switch label "Flaps", I'll soon have pictures for the motorized flap control.  I got the idea of the web, and hopefully improving on the original design.  more about that when it's completed.

motor & cover:
    This picture shows the 447 motor installed with custom cover over opening below.  I also made a heater with a cockpit controlled door using a choke cable, 4" aluminum duct, and 4" dryer vent.  My original door design was only held on one side like a standard damper in ductwork, but it took about 5 minutes of taxing around the yard for it to get pulled through the prop.  It's now got a shaft all the way through the duct. secured on both sides.  Hopefully I can leave heater on year-round and use it on those chilly Summer dawn patrol mornings.
    On the right, you can just see the chrome exhaust tip on muffler.  I saw on a web site where a guy inserted a 1-1/4" sink trap cut at 90 degrees to deflect exhaust away from prop, and tail.  I didn't like restricting the exhaust, so I used a 1-1/2" trap, and fit it over the outside, and sealed it with high temp. silicone.  Works so far.

windshield
    I used the existing windshield frame, and 3rd door, but replaced the Lexan in the windshield since it was pretty scratched up.  I added some foam tape used for sealing truck toppers to the 3rd door, to seal the gap, and I may do this to the other side as well if it's a problem.  The foam tape actually works to well, and I had to cover it with black duct tape, or it tended to stick to the side of the plane.  I will probably trim the door, and windshield with black vinyl to cover aluminum frame, and pretty it up, but that's for a rainy day.
    Note white strut fairing on floor, that's next after finishing flap control, and I think we're ready to fly.

  So far my Challenger is one heck of a good go-Kart, engine ran great around the yard, and hopefully soon into the air.

***************************************************

Motorized Flaps:
    I finally got a design that worked well, and that I was comfortable with, after numerous designs, and wasted aluminum trying different bracket configurations.  There are NO new holes drilled in root tube.  The existing bolt that holds the shoulder harness straps is used, and a second bracket goes over the root tube with a bolt through it below the root tube to squeeze it together.
 
    Of course it turned out to be very simple in the end.  There's three pictures pertaining to the motorized flap control, one is a close-up, with the components numbered, that I will describe below, the second is an overall picture, and the third is an attempt at getting a picture of the crude gage I temporarily made on the upper portion of the windshield.  After I know it works, I'll clean up the gage portion.
 
Detailed image:
1.  original pushrod, shortened.
2.  The body portion of an aluminum turnbuckle that has 1/4-20 threads.
3.  a piece of 1/8" x 2" aluminum strip bent to a 90 degree angle with a hole for turnbuckle body to pass through, and to mount motor to.
4.  small piece of aluminum angle held onto turnbuckle body with a worm gear clamp to attach plastic strip for gage .
5.  1/4-20 all-thread with motor end ground square for about 3 inches to slide into square motor drive hole
6.  used 12v motor from electric car seat assembly with a square drive hole that goes all the way through.
7.  !/4" locking collar & washer at both ends of motor drive to secure the all-thread from coming out.
8.  1/8" x 2" aluminum bracket  (U-shaped) to hold item #3 down, and secure to root tube, with holes drilled for bolt to pass under root tube.
9.  long strip of thin plastic taped to item #4 to act as gage in upper portion of windshield.
 
    The most expensive part was the 6-pin 12v switch shown in the dash picture, I think it was $12.  The used motor I got free from a local dealers service department.  I actually got the whole seat assembly they were throwing out.  The turnbuckle was under $2, and a strip of 1/8" x 2" aluminum is all you need.  I'll let everyone know how it works when I have some pictures of the plane in the air.

 

 

 

  It Flies!!!!!!!

IT FLIES !!!!!!!!, didn't get the pretty wing strut fairings on yet, but IT FLIES!!!!  I got two hours of flight time in this last weekend, and look forward to many more.  It flew just how I had hoped, and expected, GREAT, I LOVE IT!!!